MWFan
Well-Known Member
Just finished reassembly of fresh shortblock, heads were inspected by machinist, no issues.
440 +.030, 9.3/1 compression ratio, 452 stock heads, Mopar HP exhaust manifolds, 2 1/4" pipes, 484/284 purple shaft, Holley 750 Vac secondary, Mopar dual plane aluminum intake, 727, Dana 60 3:54/1,
Before I rebuilt it, I had blocked the vacuum advance and set the all in timing to 36 degrees. It had a small stumble but much better than it is now since I tried reconnecting the vacuum and setting initial timing to 12 degrees BTDC. I have gone up a step on the squirters but don't recall the number.
This is my 1st Mopar big block. Is there any common issue that I am overlooking?
440 +.030, 9.3/1 compression ratio, 452 stock heads, Mopar HP exhaust manifolds, 2 1/4" pipes, 484/284 purple shaft, Holley 750 Vac secondary, Mopar dual plane aluminum intake, 727, Dana 60 3:54/1,
Before I rebuilt it, I had blocked the vacuum advance and set the all in timing to 36 degrees. It had a small stumble but much better than it is now since I tried reconnecting the vacuum and setting initial timing to 12 degrees BTDC. I have gone up a step on the squirters but don't recall the number.
This is my 1st Mopar big block. Is there any common issue that I am overlooking?