hunt2elk
Well-Known Member
Messing around with the 400-493 stroker in my Super Bee. For those that remember, this is the second go around with this engine for me.
Built by a prominent shop in CA. The first one had a detonation issue. Pulled the motor and sent it back to get a milder cam, and dish pistons with a quench. I lost 20 hp and 4 ft lbs if I remember correctly.
Anyway, got the new motor in last winter and have put 1800 miles on it so far. Have been noticing a progressively worsening valve train noise. Everyone says that hydraulic flat tappet never need service, so I just kept driving it. Today I pulled off the valve covers and was shocked to find the adjusting nuts for #3 intake and #4 exhaust laying in the bottom of the head. #1 and #4 intake nuts were loose. #3, #5, #6 exhaust nuts were loose. The remaining 9 are tight.
What could possibly cause this to happen?
PRW rockers, Trick Flow 240 heads.

Built by a prominent shop in CA. The first one had a detonation issue. Pulled the motor and sent it back to get a milder cam, and dish pistons with a quench. I lost 20 hp and 4 ft lbs if I remember correctly.
Anyway, got the new motor in last winter and have put 1800 miles on it so far. Have been noticing a progressively worsening valve train noise. Everyone says that hydraulic flat tappet never need service, so I just kept driving it. Today I pulled off the valve covers and was shocked to find the adjusting nuts for #3 intake and #4 exhaust laying in the bottom of the head. #1 and #4 intake nuts were loose. #3, #5, #6 exhaust nuts were loose. The remaining 9 are tight.
What could possibly cause this to happen?
PRW rockers, Trick Flow 240 heads.

