Hi all,
Follow up to my posting in the Fuel and Air Systems Forum. As mentioned over there, new carb solved the issue of no squirter action. I'll dive into that carb and figure that out later.
My immediate issue is that the car starts, idles and drives (383, 4 speed), but at partial throttle it is very weak and feels like it is suffering an ignition issue. 1st gear seem OK, but I think the low gearing is hiding the issue. Immediately after shifting into 2nd, 3rd gear and 4th gear, it is just plain sluggish.
What I have done to troubleshoot/correct:
1) Vacuum Leak - none found
2) Float Levels - dribbles out of sight hole when bumping the car
3) Plug wires - all seem to be OK. Less than 1000 miles on them
4) Firing Order - OK
5) Distributor cap and rotor - seem to be fine. Less than 1000 miles on them (Distributor is a freshly rebuilt unit) NOTE: this is a converted Chrysler electronic ignition from who knows when. (See Pic)
6) Timing - ~12 degrees initial and advances as expected with increased RPM. Set with vacuum advance disconnected and plugged. I do not have a timing tape so I don't know total timing.
7) Replaced the coil with a brand new Accel Super Stock unit. (removed the Pertronix Flamethrower coil)
8) Ballast resistor - key in ON position is 5.3v in and 8.75v out.
9) Cleaned and regapped the plugs - less than 1000 miles on them. A couple were fouled.
Any assistance is greatly appreciated. Trying to resolve to go to Carlisle this week and can't drive it 400+ miles in this condition...
Thanks,
Bob
Follow up to my posting in the Fuel and Air Systems Forum. As mentioned over there, new carb solved the issue of no squirter action. I'll dive into that carb and figure that out later.
My immediate issue is that the car starts, idles and drives (383, 4 speed), but at partial throttle it is very weak and feels like it is suffering an ignition issue. 1st gear seem OK, but I think the low gearing is hiding the issue. Immediately after shifting into 2nd, 3rd gear and 4th gear, it is just plain sluggish.
What I have done to troubleshoot/correct:
1) Vacuum Leak - none found
2) Float Levels - dribbles out of sight hole when bumping the car
3) Plug wires - all seem to be OK. Less than 1000 miles on them
4) Firing Order - OK
5) Distributor cap and rotor - seem to be fine. Less than 1000 miles on them (Distributor is a freshly rebuilt unit) NOTE: this is a converted Chrysler electronic ignition from who knows when. (See Pic)
6) Timing - ~12 degrees initial and advances as expected with increased RPM. Set with vacuum advance disconnected and plugged. I do not have a timing tape so I don't know total timing.
7) Replaced the coil with a brand new Accel Super Stock unit. (removed the Pertronix Flamethrower coil)
8) Ballast resistor - key in ON position is 5.3v in and 8.75v out.
9) Cleaned and regapped the plugs - less than 1000 miles on them. A couple were fouled.
Any assistance is greatly appreciated. Trying to resolve to go to Carlisle this week and can't drive it 400+ miles in this condition...
Thanks,
Bob