As far as I can tell, it’s on ok. I think it was close to being good to go today. The adjustment procedure that Doug suggested seems to be my best option to get it working as it was. It’s so close to the end of the swivel clamp to get third but Park is touchy, and I will try slightly adjusting it opposite to split the difference and hopefully everything will be back to normal. My guess is a lot of aggravation would be eliminated if the lower rod was about 1/4-3/8” longer. I can’t remember how close to the end of the block it was, maybe it was even in a slight amount to get the park travel necessary. In the process of trying to get the adjustment done today, somehow the shifter slide in the console broke behind the shifter leaving a hole there when shifter is all the way forward and supposed to be in park. Tomorrow I will try to adjust to get shifting problem resolved, then I will look into replacing the shifter slide. Thanks to all who weighed in. I will post any news, good or bad.